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AbstractAbstract
[en] In case of loss of the residual heat removal system and other alternative cooling methods under mid-loop operation during shutdown of the pressurized water reactor plant, reflux condensation in the steam generator (SG) may be an effective heat removal mechanism. In reflux condensation experiments 7.2c with injection of nitrogen gas using the BETHSY facility in France, which is a scale model of a pressurized water reactor plant, 34 heat transfer tubes were divided into two kinds of flow patterns, which were steam forward flow and nitrogen reverse flow. In this study, we simulated the BETHSY experiments using the transient analysis code RELAP5. Modifying calculation equations for interfacial friction force and wall friction force between the inlet plenum and heat transfer tubes, nitrogen reverse flow was successfully simulated. In calculations with alteration of the flow area ratio to two flow channels for the heat transfer tube bundle, the number of active tubes with the maximum nitrogen recirculation flow rate agreed rather well with the observed number of active tubes. In calculations with three flow channels for the heat transfer tube bundle, the average number of active tubes in several calculations with different flow area ratios of the three flow channels predicted the number of active tubes well. (author)
Primary Subject
Source
11 refs., 17 figs., 5 tabs.
Record Type
Journal Article
Journal
INSS Journal; ISSN 1340-4482;
; v. 14; p. 373-383

Country of publication
BOILERS, COMPUTER CODES, COOLING SYSTEMS, ENERGY SYSTEMS, ENERGY TRANSFER, ENRICHED URANIUM REACTORS, FLUIDS, GASES, MATHEMATICS, POWER REACTORS, REACTOR COMPONENTS, REACTOR COOLING SYSTEMS, REACTORS, REMOVAL, SHUTDOWN, THERMAL REACTORS, VAPOR GENERATORS, WATER COOLED REACTORS, WATER MODERATED REACTORS
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